侯立中, 谈心, 曲洪娜. 加拿大Daylight油田致密砂岩油藏优快钻井技术[J]. 石油钻探技术, 2014, 42(2): 52-56. DOI: 10.3969/j.issn.1001-0890.2014.02.011
引用本文: 侯立中, 谈心, 曲洪娜. 加拿大Daylight油田致密砂岩油藏优快钻井技术[J]. 石油钻探技术, 2014, 42(2): 52-56. DOI: 10.3969/j.issn.1001-0890.2014.02.011
Hou Lizhong, Tan Xin, Qu Hongna. Optimized Drilling Technologies for Tight Sandstone Reservoirs in Canada Daylight Oilfield[J]. Petroleum Drilling Techniques, 2014, 42(2): 52-56. DOI: 10.3969/j.issn.1001-0890.2014.02.011
Citation: Hou Lizhong, Tan Xin, Qu Hongna. Optimized Drilling Technologies for Tight Sandstone Reservoirs in Canada Daylight Oilfield[J]. Petroleum Drilling Techniques, 2014, 42(2): 52-56. DOI: 10.3969/j.issn.1001-0890.2014.02.011

加拿大Daylight油田致密砂岩油藏优快钻井技术

Optimized Drilling Technologies for Tight Sandstone Reservoirs in Canada Daylight Oilfield

  • 摘要: 为经济高效地开发致密砂岩油藏,并为国内同类型油气田开发提供借鉴,进行了Daylight油田优快钻井技术研究。对Daylight油田地层岩性进行了研究,根据地层压力优化了井身结构;通过分析测井资料并结合统计数据,研制了个性化的钻头;在分析钻井技术难点、地层压力的基础上,研制了油基钻井液体系,并采取严格措施确保其性能稳定;采取防碰技术控制井眼轨迹,满足了井工厂钻井的要求;优选先进的井下工具进行配套应用。该油田油气井井身结构按地区简化为二开和三开2种;研制了适应该地区软硬交错地层的复合钻头;油基钻井液体系为井壁稳定提供了保障;提前防碰技术缩短了滑动钻进时间;振荡钻井技术和AGITATOR井下工具可以解决水平井钻井中的托压问题,黑匣子为分析钻柱涡动提供了数据支持。应用结果表明,同地区平均井深为3 000 m的井,平均钻井周期由原来的18 d缩短为8 d。Daylight油田优快钻井技术研究为快速钻井提供了保证,为国内致密油藏开发提供了技术参考。

     

    Abstract: In order to develop tight sandstone reservoirs economically and efficiently,and provide references for development of similar oil and gas fields,the drilling technologies in Canada Daylight Oilfield have been investigated.By analyzing main affecting factors on optimized drilling technologies,some important achievements have been obtained,including casing program optimization on the basis of formation pressure;specific bit developed through logging data analysis and statistics;oil-base drilling fluid system developed through the analysis of drilling troubles and formation pressure,and anti-collision drilling techniques were taken to control wellbore trajectory,so as to meet the requirement of well factory drilling;Optimization of advanced downhole tools for matching application;wellbore structures are simplified as two forms,i.e.second spudding and third spudding sections;the composite bits for the alternative hard and soft formations were developed;oil-base drilling system provided safeguard for well bore stability;anti-collision in advance reduced the sliding drilling time;vibration drilling and AGITATOR downhole tools solved the BHA drag,black box provided real data analysis for the vortex of drill string.The study results show that drilling time of average 3 000 m wells in the area were reduced from 18 days to 8 days.The optimized dril-ling technologies provide a guarantee for fast and optimum development of Daylight Oilfield,and good re-ferences for efficient development of tight oil and gas fields in China.

     

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